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30 April 2008
I've updated the Z10000 Assembly and Operations manual to
reflect the new component packaging and also updated and expanded performance
measurements. I also fixed a couple of errors pointed out by builders.
It may be downloaded by clicking
here or via the Documents page. The new
manual is version 3.0 and has the same file name as the older manual.
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28 April 2008
I spent most of the weekend making performance
measurements on a K3-IF Softrock Lite 6.2. I don't know if I will post the data
to a new web page in the next few days or wait until my K3 arrives so that a
complete analysis is possible.
Today was occupied in assembling kit packages for another
batch of Z10000s. The photo below shows how I handle the surface mount
resistors. The blue tray is a bead storage box with 32 round bottom bins,
purchased at the local Michaels Arts and Craft store. I cut each resistor
section from the longer tape with the short scissors in the photo.
As a cross check on accurate packaging, I double count the
resistors when I cut and place them in the bin. If all goes well, all bins empty
simultaneously. I use a similar process for the rest of the components.
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Z10000 kit Surface Mount Resistors to be Individually
Packaged
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25 April 2008
More maintenance this week. This time, a piece of
quasi-consumer electronics with a throw-away design.
I bought a Magellan MAP 330 GPS around 1998, and have used
it quite successfully since. However, the control buttons have gotten
progressively less reliable and a few months ago the "enter" button ceased to
function. Enter button failure made the MAP 330 unusable, as the screen
after power-up gives you five seconds to hit the enter button, by which action
you acknowledge that the data provided is for entertainment value only, etc. The
"lawyer screen" in other words, although I sincerely doubt this disclaimer would
prove all that useful. After all, one does not purchase a GPS receiver for
entertainment; nor does the manufacturer sell them as entertainment devices.
Regardless, without a functioning enter button, the GPS is
unusable; it automatically turns off five seconds after turn on. I called
Magellan's service center and found that the MAP 330 is no longer supported. The
best deal they offered is a trade-in on a refurbished current production GPS,
but the price after trade-in turned out to be about the same that a new model of
the replacement current production model could be purchased from a discount
supplier.
With the understanding that the value of my
non-functioning MAP 330 is zero, I undertook a repair. The problem was
reasonably obvious; the printed circuit board pads mating with tactile control
buttons elastomer pins were likely were dirty or corroded.
The first problem is disassembling the case. My experience
is that consumer plastic cases are either held together with screws or plastic
melted rivets, often hidden under stickers. Or, if not screwed or riveted, tabs
and mating slots are used.
After removing stickers, no screws or rivets were to be
seen. Likewise, twisting and inserting a thin bladed screwdriver between the
front and rear case housings showed no signs of tabs and slots. Rather, it
seems that the case, made of polystyrene, had the two halves glued
together. This makes for a waterproof case, but also makes a clean repair job
impossible without a new case.
Still, since the defective MAP 330 was worth nothing, I
used a cutoff blade in a Dremel tool to slice around the case parting line. I
tried to cut as carefully as possible, as it was impossible to know how much
clearance existed between the case and the PCB.
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MAP 330 with the case cut in half. The white surface is
an insulator and the PCB pads for the keys are in the insulator holes.
When in this state, I was able to activate the keys by
pressing a metallic conducting rod through the holes to short the pad
fingers.
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Front of rubber key pad, showing 10 years of accumulated
grunge.
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Back of keypad. The round black holes are actually
molded pins of conductive rubber that project through the holes when
the corresponding key pad is placed. I measured about 600 to 1000 ohms
across the pin.
Frequently used keys, such as the power on, the
infamous enter key and the escape key have double rods for increased life.
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I removed the plastic insulator from the main PCB and gently
cleaned the mating PCB pads with GC's "no-oxit" contact cleaner using a cotton
swab. The photo is after cleaning. There was an extensive black reside built up
on the enter pad as well as several other pads.
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Enlarged view of the switch pad.
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In case you are curious about the rest of the PCB, here
it is. The large black cylinder is a sounder. The antenna can just be seen
at the bottom left of the photo. It's a quadrifilar helix, I believe.
At 1500 MHz, it isn't all that large.
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At this point, I reassembled the MAP 330, holding it
together with a pair of rubber bands. It worked perfectly, but the rubber bands
were not the long term solution. I
trimmed the worst of the melted polystyrene from the case halves, as I found the
Dremel tool's cutoff wheel melted the soft plastic as much as it cut it, and ran
a bead of neutral cure (non corrosive) Dow Corning silicon rubber around the
gap.
It certainly isn't as pretty as before my repair, but the
case halves hold together reasonably well. And, if another repair is required,
the silicon rubber can be cut open with a sharp hobby knife and the bead peeled
off.
While I had the case apart, I added a diode and series
resistor to charge the batteries when powered from an external supply. I
generally use the MAP 330 in my pickup truck, powering it through a Magellan
accessory socket power supply. This puts out 3.9 volts, while the 2400 mAH NiMH
AA cells I use in it are about 2.8 to 2.9 volts for the series pair when fully
charged. I sized the resistor to trickle charge the AA cells at about 15
mA.
What I find irksome about this repair is that Magellan
designed the MAP 330 case so that it had to be destroyed to be opened. This
design permitted the case to be spash-proof and certainly discouraged people
from trying to repair it with a jackknife. But, it's still annoying that a
simple repair that took no more than 5 minutes once the case was opened turned
into a two hour effort, almost all of which involved destroying the case and
cobbling together a fix. That's not good engineering in my view. It may be
excellent marketing, as it would have forced most MAP 330 owners to scrap their
units and replace them, of course.
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Post-repair, with a white bead of non-corrosive Dow
Corning silicon rubber holding the case together.
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23 April 2008
I've owned a Cubic R-3030 LF/MF/SW receiver for seven or
eight years now. It's a dual receiver, two completely independent receivers
sharing a common enclosure. The military version of the R-3030 is an R-2411 and
Cubic makes the instruction manual for it (with schematics omitted) available at
http://www.cubic.com/cda1/Prod_&_Serv/techmans/pdf/r2411/R-2411%20MANUAL.pdf
should you be interested in more information on the receiver.
A few days ago, the left side receiver failed to power up,
and I spent some time troubleshooting it over the weekend. I thought it might be
interesting to show how "the big boys" do their receivers—it's quite a
comparison to even high end amateur radio gear.
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R-3030 receiver
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First, every section of the receiver, except for the front panel is in a
separate shielded, plug-in module.All but one of
the modules has an LED "fault lamp" at the top, which illuminates if the module
is defective. Of course, not all failures can be detected, but it's surprisingly
helpful.
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Each independent receiver has 13 shielded, replaceable
modules.When the modules are installed in the
correct order, the black strip is straight.
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In my case, the problem was the left side power module, which I confirmed by two
methods. First, the power supply module fault lamp was illuminated. Second, I
swapped the right side module with the left side module and the trouble followed
the module. So far, so good.By the way, a condensed
troubleshooting guide is printed on the inside of the top cover, a small portion
of which is illustrated below.
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Power supply module. The switch selects 120/240 V AC
power. There is no fuse in the module; the power switch is actually a
combination power switch and circuit breaker.
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Power supply with the top cover removed. The enclosure is
a casting, drilled and tapped for the shielding screws. AC arrives
over the connector at the left; DC out through the right side connector,
which is a DB25.
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This is, somewhat surprisingly, a switching power supply. The AC section is to
the left of the transformer and the DC at the right.
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AC and Primary DC section of the switching power supply.
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Working on switching power supplies is not my favorite recreation for two
reasons. First, the AC and DC primary circuitry is directly connected to the AC
power mains. Second, switchers are notorious for devilishly complicated feedback
mechanisms, particularly during startup.The direct
AC mains connection imposes a major electrical shock risk, and also makes it
difficult to use normal AC powered test equipment. Fortunately, I have an AC
isolation transformer and was able to ground the primary side's floating
negative, thereby allowing me to use an oscilloscope and other normal test
gear.
In this case, the power supply was dead; would not start.
After some troubleshooting and head scratching, I decided that the most likely
failure was the UC2842 switching power supply controller IC, the large
square at the schematic's bottom. The questionable part had a 1985 date code, so
I didn't have high hopes that I could find a replacement without going to an
obsolete parts house. Surprisingly, I found the UC2842 in current production by
Texas Instruments and other manufacturers and I ordered several replacements Monday. While I had the
module apart, I removed the old part and added an 8-pin DIP socket. Sockets are
a mixed blessing for ICs, as a significant number of failures can be directly
attributed to poor pin-to-socket connections. On the other hand, it is certainly
much easier to replace an IC in a socket than one soldered in place.
I was not 100% confident of my troubleshooting, however,
so I also ordered replacements of the other possible bad parts. Here I had less
luck finding exact matches. In particular, the switching MOSFET is a Siemens
BUZ-57A which is no longer manufactured. It's in an odd case, resembling a
plastic cube with a metal mounting flange. You can see the flange bottom in the
photo, as I had to remove it for access to the UC2842. I found several other
MOSFETs with similar ratings (1000V, 4.2A) but in conventional TO220 packages,
and I ordered a couple figuring that in the worst case, there was enough room to
make it fit.
My parts arrived today and installing the UC2842 in the
socket cured the problem. After a few hours of on-time, all seems normal.
The R-3030 is an interesting receiver, with many useful features. However, the
designers had an off day when it came to the AGC section. Its attack time is
too slow (around 15 ms, instead of the necessary under 5 ms) and although
the decay time is selectable at .25, 1.0 and 3.0 seconds, all three options seem
to have the same fast decay, measured in tens of milliseconds. Both receivers
act identically, so it's not a fault in one side. The elastomer keypad is
another annoyance as it requires the fingers of a safecracker to enter data
without error.
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20 April 2008
I've tinkered with the
Using Softrock as a
Panadapter for the K2 page. More usefully, I've added a section showing what
comes out of the K2 IF port and how the out-of-band signals may be knocked down
with a Z10010-K2 bandpass filter.
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20 April 2008
I've recently acquired two HP 8657A synthesized RF
generators and made quick and dirty phase noise studies today. The data includes
comparisons with HP8640B, Panasonic VP8191A and Boonton 102D signal generators.
And, for curiosity, I also ran a similar check of my Electraft K2 transceiver's
receiver phase noise. Data at
Signal Generator Phase
Noise and Elecraft K2.
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19 April 2008
I've added a new page "Using
Softrock as a Panadapter for the K2" with photos and test results. Based on
this data, the Z10000-K2 buffer amplifier can be run as recommended in the
assembly manual; to provide around 0 dB net gain.
This new page represents a week's work in building and
testing the Softrock.
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17 April 2008
I'm continuing to work on the two Softrock Lite IF
frequency evaluations. Yesterday, I tried an EMU-0202 USB-connected sound card
with my new Dell laptop computer. (See my
Softrock page for more information on the EMU-0202.) I'm seeing some strange
behavior with the Dell, whether connected via the EMU-0202 or the Dell's
internal soundcard—an audio "reset" every few seconds. This may be a laptop
issue, or it may be in the connecting cables or other hardware. I hope to find
the problem source later today.
I've also expanded by test equipment collection by adding
two HP 8657A synthesized signal generators. One of my projects is a web page
comparing my various RF signal generators for stability, phase noise and the
like. No question that my HP 8640B is the cleanest source, but the 8640B is a
mechanical engineer's dream, chocked full of gears and cams, with custom
switches. The 8640B's are coming up on 30 years old now and the plastic gears
commonly fail, and the printed circuit board switches stop working as well. My
main 8640B no longer has functioning FM modulation, which I believe is a
defective FM modulation switch, and my military surplus 8640B (option 323, no
phase lock) has a defective bandswitch cam.
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12 April 2008
I have now assembled two "official" Softrock Lite 6.2 IF
frequency kits. One for the K2 and one for the K3. I've made preliminary
measurements on both but it will be a few more days until I can mount the two
Softrock receivers/panadapters in enclosures and run full tests.
I can confirm that the K2 version is around 11 dB less
sensitive than the K3. This is expected because the K2 uses 3rd harmonic
sampling, which has a theoretical sensitivity penalty of 9.5 dB. I measured a
bit over 11 dB sensitivity reduction compared to a 10.125 MHz Softrock Lite
6.2 I built last year. The K3 version uses normal sampling and has similar
sensitivity to the 10.125 MHz Softrock.
I can also confirm that the Z10000 is quite effective at
reducing local oscillator leakage out of the Softrock K2 and K3 receivers, but
until I mount the two Softrocks in the die cast enclosures, with filtered power
supply, etc., it's difficult to make repeatable leakage measurements.
I have a couple of die cast enclosures ordered and expect
them to arrive in five or six days.
Whether the 11 dB sensitivity loss in the K2
Softrock is important, and whether you will wish to make up that loss by
increasing the Z10000's gain remains to be seen. The Softrocks are quite
sensitive receivers, with a minimum detectible signal in the 0.1 to 0.2
microvolt range. Even with an 11 db sensitivity loss, there's likely more gain
at 4915 KHz than necessary, except perhaps under extraordinarily quiet
conditions, or, perhaps, for weak signal VHF/UHF operation. I'll
make measurements with the K2 Softrock connected to my K2 as part of the
complete test. I don't have a delivery date for my K3, although the second
receiver problem seems well on the way to being fixed, which brings my K3 closer
to arrival, as the second receiver is the delaying factor.
The photos below are two of last week's visitors to our
front yard.
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10 April 2008
I've added a section to the
Z10000 page showing how I mounted two of the
amplifiers in Hammond die-cast enclosures and presents swept frequency response
data for the amplifiers. The result is a useful general purpose laboratory
amplifier with 10 dB gain from 3 KHz to 175 MHz.
I've also added a table of contents with jump links to the
Z10000 page to help navigation.
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08 April 2008
I've added 3rd order intermodulation measurements of a
Z10000 amplifier to the Z10000 page.
The short story is the amplifier shows an IP3 intercept of
+36 dBm, an impressive number.
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07 April 2008
I've had a couple international customers pay via
International Money Orders, denominated in US$ recently. It turns out that my
bank (BB&T) assesses a $5.00 "service charge" for depositing International Money
Orders. Hence, I have to ask international customers wishing to pay with an IMO
to include the US$ 5.00 fee.
PayPal is much more efficient in this case, with a decent
foreign exchange rate and no international surcharge.
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06 April 2008
I've added a section to the
Z10010 bandpass filter page describing
how I tune a filter.
After looking in out-of-the-way storage, I found two 4915
KHz (K2 IF) frequency bandpass filters that I had partially completed in 2006
but didn't need at the time. I'll finish those filters over the next couple
days. I also found one complete 4915 KHz filter from my 2006 production, so I'll
be able to ship three K2 filters this coming week.
I also built three 8215 KHz (K3 IF) bandpass filters with
the last three 2006 PCBs and they will also be shipping this coming week.
Additional filters will be available when the revised PCBs
arrive, still scheduled for mid-April.
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05 April 2008
I've been asked how one acquires a Softrock Lite kit to be
used as a panadapter for the K2 or K3. Tony Parks, KB9YIG, "Mr. Softrock"
replied to my query as follows:
Hi Jack,
Yes, I can supply both of the IF kits you
list below at a price of $12 per kit. The K2 IF kit has a 4.898 MHz
center frequency and the K3 kit has a 8.191 MHz center frequency.
You can send Tony the appropriate funds to his E-mail
address raparks@ctcisp.com and you will
soon receive your Softrock kit.
I'll add this information to the
Z10000 page as well.
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05 April 2008
I've received confirmation from Bob Friess, N6CM, that the Z10000's isolation
is well above my earlier quoted 70 dB:
Hi Jack,
The amplifier seems to work very well. I am limited here in the desert by
an old analog network analyzer, but S12 is something greater than 80 dB.
Bob
S21 is, of course, reverse isolation, signal applied to port 2 (output),
measured at port 1 (input).
Hence, the correct isolation is in 80-90 dB range, as it's now clear my lower
quoted figure must have been made with the power inadvertently disconnected.
I've added a correction note to the Z10000 page.
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04 April 2008
Yesterday and today have been occupied with getting
Z10000 orders out. To show part of the process, I took a few photos during
construction of the SMA bulkhead cable supplied with the internal installation
option. I assembled 12 cables today in the space of 4 hours, or 20 minutes a
cable. I include a couple of breaks to check my E-mail in this time, so
that actual per-cable time is closer to 15 minutes, which is an embarrassingly
slow pace.
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RG-178 Teflon coaxial cable cut into approximately 2 foot
lengths.
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Ratcheting crimp tool, with interchangeable jaws. I made
the drawing and instructions as the connectors came with little to no
documentation.
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My SMA connector storage box
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Tools needed to assemble the connectors. A decimal inch
scale and a sharp pointed pick for combing the braid back are necessary.
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Stripping the outer jacket with Hakko FT-800 thermal
strippers. I've set the depth gauge to the correct depth. As a backup
measure, I've also made a mark on the jacket with a black permanent marker.
The thermal strippers yield a clean cut, with no risk of
nicking the shield. I also use the thermal strippers for the center
conductor
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The parts that go into the bulkhead connector. The small
white plastic insulator has a habit of getting lost.
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To solder the center conductor, I use a piece of
Teflon rod, drilled to hold the center receptacle. This arrangement
frees up both my hands for soldering.
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Crimping the outer conductor.
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Applying the heat shrink tubing boot over the connector.
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Before I crimp the connector in place, I check the cable for shorts and opens. I
check it again after criming and heat shrink application. Between the initial
run in 2006/7 and the second run, I've had to scrap two connectors out of
about 65 assemblies. In both cases, the problem was a short, which I believe was
caused by one of the center conductor strands not making it into the solder
hole. This has lead me to the pre-crimp check for shorts and opens.
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02 April 2008
As usual, I've moved the March 2008 page to archives,
reachable by clicking here, or via the navigation
table at the top of this page.
I shipped nearly 20 Z10000 buffer amplifiers today, in
various configurations. Interestingly, about half the Z10000 purchasers are
international. That's quite a bit greater than my experience with the Z100,
where international orders were around 20% of the total. Given the current
US/Euro exchange rate, US products are a bargain compared with historical
exchange rates. |