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125 KHz Low Pass Filter

I was recently asked to design a one-off 125 KHz low pass filter, intended to improve VLF reception by reducing interference from non-directional beacon and medium wave broadcast stations.

Since the filter is a one-of-a-kind design, I used prototype techniques to build it.

The filter design and component values is shown below. (I used AADE's filter design software for this filter. http://www.aade.com/filter.htm) The filter is a 7th order Butterworth low pass filter, designed for 50 ohms in/out impedance. Since the filter will be used in an environment with unknown drive and termination impedance, a Butterworth filter is a reasonable choice. The purpose of the filter is to remove medium wave and non-directional beacon signals from a computer sound card connected to a Z1501 active antenna. Sound cards often don't have good low pass filtering when hit with signals in the MHz and above range and an auxiliary filter is necessary to remove artifacts.

 


At 80 and 127uH, the inductors are uncomfortably large for reasonable size powdered iron cores and hence ferrite core inductors must be considered. Of the commonly available ferrite material, Fair-Rite mix 61 is my preference for filters over the range from a few KHz through 10 MHz or more. 61 material permits inductors with decent Q and a reasonable number of turns in a compact form.

After evaluating several possible core sizes, I decided to use "double stack" FT50-61 cores. A double stack core consists of two cores glued together to make a core twice as tall. First clean the cores with denatured alcohol and allow them to dry. Then liberally coat one core face with cyanoacrylate adhesive (also known as "super glue"). Place the second core on top of the first and allow the adhesive to set up.

A double stack core has an AL value twice a single core and hence reduces the number of turns required to 70.7% of the number required for a single core.

The 79.3 uH inductors required 25 turns of no. 26 AWG magnet wire (30 inches of wire) and the 127.3 uH inductor 31 turns of no. 26 AWG (40 inches of wire). I normally use thermal strippable magnet wire for powdered iron cores, but uncoated ferrite cores, such as FT50-61 cores, will abrade the insulation and result in wire to core contact, which is undesirable. Instead, I used Belden 8079 "armored thermaleze" magnet wire, with a amide-imide polymer top coat. The top coating makes the wire highly resistant to scrapes and abrasion and is a good choice for uncoated ferrite cores. However, the insulation must be mechanically removed and cannot be thermally stripped by dunking it into a solder pot.

After winding the three inductors, I coated them with Q-Dope to hold the windings in place. The measured inductance values (at 100 KHz, measured with an HP 4192A LF Impedance Meter) were:

L3: 79.22 uH Q=101.2
L7: 81.27 uH Q=100.3
L5: 124.33 uH Q=100.5

L7 and L5 differ from the target inductance value more than I would like, but the normal strategy of compressing or stretching the winding over the core perimeter produces only tiny changes in inductance in a high permeability core. Hence, the only way to change inductance by an appreciable amount is to add or remove turns, and in this case changes in turns would produce even larger divergence from target values.

To compensate for errors in the inductors, the capacitor values can be adjusted. To accomplish this, I measured the three inductors at the two "dipole frequencies" identified in the filter design. From the measured inductance values, the resonating capacitance can be determined. This yields two values for C4 and C6, and the average of the two values can be used to split the error.

Example:

L3 & C4 resonate at 83.4 KHz. Based on L3's value measured at 83.4 KHz, C4 should be 46090pF

L5 and C4 resonate at 65.9 KHz. Based on L5's value measured at 65.9 KHz, C4 should be 46930pF

C4 is thus selected as the average of the two computed values; (46090 + 46930)/2 = 46510 pF

46510pF is made up with 4 10000pF polystyrene capacitors plus two selected 3300 pF capacitors. (All capacitors are measured and hand selected.)

I built the filter on a piece of scrap printed circuit board material 3.50 inches x 1.875 inches with four holes to fit inside a Bud PI 1905 LG enclosure.

I used a 5/16th inch diamond "core drill" to cut four isolated pads in the PCB material to serve as junction points for the inductors and capacitors.


The completed filter is pictured below. It has a total 16 capacitors and is not a suitable construction technique for a filter with a corner frequency in the MHz range. But, it's fine for our 125 KHz filter.

I've mounted the center inductor at right angles to the end inductors to reduce unwanted magnetic coupling.

 


I mounted the assembled filter in the enclosure and added BNC connectors. The enclosure is plastic, which makes it easy to machine.

 


The completed filter enclosure.

 


The measured performance is quite close to the design software. The predicted -3 dB point is 125 KHz, and at 125 KHz, the measured insertion loss is 2.9 dB.

At the bottom end of the medium wave band, 540 KHz, the filter has a loss of 81 dB, rising to 72 dB at 2 MHz. There are several reasons why the filter exhibits blowby at higher frequencies. One is that the 61 ferrite material becomes less useable as the frequency increases. Secondly, the inductors have distributed capacitance which degrades the filter into a simple capacitor ladder network at frequencies well above the inductor self-resonant frequency. Thirdly, the polystyrene capacitors have self-inductance which  reduces their value at higher frequencies and fourthly, there is some loop coupling between the two BNC connector attachment wires.

Still, the result is quite usable, with at least 55 dB attenuation at 30 MHz.

 


The plot below shows an expanded view (1 dB/division) of the passband. The passband insertion loss is close to zero (0.016 dB) at mid-band (53 KHz), dropping to around 0.8 dB loss at 5 KHz.